lillian
lillian
RRCRat Rig Community [Unofficial]
Created by lillian on 4/4/2024 in #fix-my-printer
probe deployed but error triggered
got a problem with an euclid probe that worked previously, it can't home as it return an error as if triggered or as if the probe wasn't attached so i checked the wiring (shitty dupond connector) redid it using hot glue so no wiggle and still the same as soon as it pick the euclid from the dock it trigger the security mode
7 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 2/12/2024 in #fix-my-printer
ERROR c0130010
Hi my printer developed a new bug it was working and from one print to the other it got the error: "TMC 'stepper_x' reports error: DRV_STATUS: c0130010 s2vsa=1(ShortToSupply_A!) cs_actual=19 stealth=1 stst=1 Once the underlying issue is corrected, use the "FIRMWARE_RESTART" command to reset the firmware, reload the config, and restart the host software. Printer is shutdown". first time i checked the wires and the connection and restarted just fine ... one print later it came back i got this error code in the start sequence i don't understand where it came from i had this bug once like 6 month ago and it went away by itself i dont understand what could cause such an erratic problem...:pepehands:
14 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 2/7/2024 in #ratos-support
webcam and dumb user
hi mostly guys and girls i can't get my system to connect a webcam i tried 2 time followed several guides and looked at this discord and the mainsail one and still can't figure what is wrong... i got an error on moonraker i thought it was a due to the fact i haven't done the update and the the updates corrupted itself and so i ended up re installing the whole printer, what do you think went wrong ? and can someone link a install protocol that is up to date
2 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 8/22/2023 in #fix-my-printer
MCU LOST CONNECTION and now can't connect to rat os
hi guys again and again with this printer cant have 2 weeks without problem, the new one : error code before i shut down and now cant get to rat os : " Can not update MCU 'mcu' config as it is shutdown Once the underlying issue is corrected, use the "FIRMWARE_RESTART" command to reset the firmware, reload the config, and restart the host software. Error configuring printer , could it be connected with the fact that my pi send me an undervolted error code (as it is clearly not with 5.1v buck converter)
3 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 8/16/2023 in #fix-my-print
idea maker launch on print fail
since trying out ideamaker i can't figure out how to launch a print i get this error: 15:41 Unknown command:"T0" 15:39 Unknown command:"M99123" i think it is a raised3d specific command for their printer but i changed the start gcode / end g code on the filament profile and also on the printer profile i dont understand where this line came from. after this 2 lines the printer don't do anything as i am not yet good on this slicer i check here for help as anyone found this problem and solved it?
1 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 6/27/2023 in #fix-my-printer
X Y slipping skipping or other
No description
33 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 6/21/2023 in #fix-my-printer
Move out of range on mesh
my config forced me to make change that induce other problem latter as this one: i run a euclid probe with a phaetus volcano so i needed a custom doc and bracket to go around the volcano duct, and doing this the bracket was going to collide with the frame on the x axis, it was sticking further than the endstop so i moved the endstop out 7mm. and so i overide the x max range to 490 instead of 500 (+3 mm for piece of mind). but when running a mesh the combination of the probe big offset (-45 x an -5 y) and reduce X range throw me a : "Move out of range: 509.960 25.000 5.000 [0.000]" what would be the smart way of solwing that ? reprinting a duct and mount or trying to overide the mesh ?
7 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 6/20/2023 in #ratos-support
shut down due to euclid state
i get an error message when trying to home the printer caused by the euclid: the same as @nanserbe on is post from 06/03/2023: "Shutdown due to expected probe state to be deployed but is stowed (1) Once the underlying issue is corrected, use the "FIRMWARE_RESTART" command to reset the firmware, reload the config, and restart the host software. Printer is shutdown" i tried his solution: modifying the pin to correspond to my wirring (5v probe type) but i still get the error. on the mecanical aspect of things the printer move flawlessly no skipping step or anything. if someone know the fix id be happy to know too
137 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 6/2/2023 in #ratos-support
ratos vanished
after much complication i finaly got my set up to work and then i could not connect or find ratos.local , can't find the pi on my router and the ratos hotspot asn't pop backup. any clues?
32 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 5/5/2023 in #ratos-support
mcu not connecting
i re wrote my post as it as been deleted ... i was having problem to connect and flash an octopus v.11 and after much testing with the great help of @Helge Keck (many thx again) to diagnostic the problem it seems that the octopus not responding was a problem of the board. i reopen the post as i have development on the matter: thinking that the board was bad and waiting for another one i tried to put the pi4 on an ender 3v2 with an v4.2.7 board... trying to install klipper i runned in some problem: mcu not connecting maybe another bad board i tried a third one and same so maybe the problem came from the pi: the problem came from when ssh into the pi looking for " ls /dev/serial/by-id/" following the procedure >>> https://www.klipper3d.org/Installation.html never the pi responded the correct answer but when trying "ls /dev/serial//*" the pi found a connection and when swaping this answer into printer.cfg i go the bord to respond and connect: every thing was running fine. so my question is how knowing that could we try to make ratos work on the octopus or should i just go and run basic klipper
10 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 4/24/2023 in #ratos-support
can't connect to mcu
after a full reinstall/ flash of the pi and the btt octopus v1.1 i still get an "Klipper reports: ERROR mcu 'mcu': Unable to connect"
145 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 4/20/2023 in #ratos-support
can't access back on http://ratos.local/
i was finalizing my config and went aways for a few day on another project and now i can't access back on to http://ratos.local/
22 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 4/12/2023 in #fix-my-printer
motor return error code
when trying the first start up of the printer following the procedure i tried to over ride he motor with "SET_CENTER_KINEMATIC_POSITION" to check their movement and i get a error and the return: TMC 'stepper_x' reports error: DRV_STATUS: c0130010 s2vsa=1(ShortToSupply_A!) cs_actual=19 stealth=1 stst=1 i checked the wires and the plugs both side are good... more over the gantry was, as i first talk about in "sticky axis" post of @gsieben, kind of hard to move i rechecked as recommended on that post the diagonals and they are both equal ... i dont understand either problems and their relations
9 replies
RRCRat Rig Community [Unofficial]
Created by lillian on 4/12/2023 in #fix-my-printer
end stop and probe shenanigans
hello i am kind off clue less on a problem i have with my new config: ratrig vcore / octopus v1.1 / euclid probe / raspberry pi4 // all on mainsail the problem is after the initial programation when i got to checking endstop (i followed the klipper procedure) they returned: all triggered. i proceded to check if it was a state inversion with: QUERY_ENDSTOPS , and the result is the real problem: Z (euclid probe) return triggered manualy activated or not. also X & Y are on open when manually triggered and triggered on their default state i know i need to change the pin comment with a "!" or remove it but i have no clue where to find this line of code as it is not in the doc "printer .cfg". Soi checked if the placement on the board was good for the euclid: https://os.ratrig.com/docs/boards/btt/octopus-11/ also the euclid probe its a basic switch and its wirred on the correct emplacement on the board: image may the problem be : i quote the euclid probe site "If Euclid Probe is to be wired to the Probe Port (pin PB7), you may need to set the probe pin LOW in order for the firmware to recognize the operation (~PB7). See Section 2.7 in the Octopus User Guide under Probe Port Wiring"
link https://www.roboter-bausatz.de/media/pdf/b1/e2/b3/BIGTREETECH_Octopus_EN_updated_0719.pdf so i checked and it seems to be an "PnP" type probe if i am not mistaken (open state >> sig is link to gnd and when closed it is not so it must be on power ) (Rq: opposite from the end stop i have .... that seems weird for me) and from there i am lost on what i should do... i hope this was clear enough and thanks for the time some will pass on this topic
30 replies