vcore 3.1 prints fine with prints that are up to 3 hours But with longer prints 5+ it layershifts
Title says everything. Printer is 3.1 300mm with rapido uhf hotend. Just default set up basically. and rat os 2.1 most updated version.
45 Replies
does it layershift once, or at that point is it all over the place?If you print something tall does it fail at the same height?
So when i print something tall so for instance around the max height it can be fine. but it just the longer prints that fuck up
wait
here is what i mean left
fine
right fucked
have you calibrated your infill extrusion? I've seen people have that be over extruded which then causes a nozzle to drag and bump and cause a layer shift
oh! good call
I havent actually
whats the best way to do that
try doing a print with Z hop enabled. If it prints fine that would be a good indicator the nozzle is bumping something and to do more extrusion tuning
It seems
i already have zhop enabled
how tight are your belts?
And do you have fans over your stepper drivers?
tension on touch doesnt feel to tight. I cant check the graph because the macro doesnt wanna work with beacon havent come to that yet
and no i dont have fans but never needed them on my other bigger printer 500mm
I can put a fan on it. i have a big be quite 12 v fan
are you using "performance mode"?
you need to get that fixed, people often over tighten them. Feel means nothing
Do you know how to get the beacon to work as the graph measurer
I dont have anything else
To check it
8:18 PM
Invalid adxl345 id (got ff vs e5).
8:18 PM
Invalid adxl345 id (got ff vs e5).
This is generally indicative of connection problems
(e.g. faulty wiring) or a faulty adxl345 chip.
8:18 PM
Invalid adxl345 id (got ff vs e5).
8:18 PM
Invalid adxl345 id (got ff vs e5).
This is generally indicative of connection problems
(e.g. faulty wiring) or a faulty adxl345 chip.
8:18 PM
RatOS: All requested axes already homed, skipping..
8:18 PM
MEASURE_COREXY_BELT_TENSION
i get this error
are you specifying the beacon ADXL? I can't tell since you didn't provide the logs
which log do you want
my printer.cfg
please attach a debug zip (which you can download from the sidebar in the configurator) to your post.
oke
moment
looks like it is sometimes working, so I would blame wiring or connection for your ADXL issues
also looks like you don't have performance mode enabled. It really is "normal mode" and non performance mode is "handicap" mode just meant for ensuring your motion system is working. Get some fans on your stepper drivers and enable performance mode
Ah oke
How can i connect a 4 pin 12 v fan
I mean if i connect only the 12v and the ground it will be constantly on
but where do i put the pwm or tachmeter
Are you running an octopus?
Connecting a 4028 fan | RatOS
4028 server fans are becoming a popular option for part cooling because of their light weight and great pressure and flow rates. In this guide we'll go over how to connect one and use it for part cooling. 4-pin fans usually aren't used in 3d printers, and many boards only provide 2-pin ports, but fear not! There's always a way.
I am actually
but i want to use this as the stepper cooler
I don’t think it offers any benefit for that application over a 2 wire fan
its the only one i have
to be honest
thats the reason
Ah
Well that link above will get you what you need. I also wouldn’t bother wiring up the tacho
How do i do custom fan name
i plugged in this fan
and its working
but its not spinning fast
at all
Maybe somebody can recommend me a stepper cooler fan
[controller_fan stepper_cooler] # Stepper motor cooler fan
pin: PD14
cycle_time: 0.0001 # Try reducing this value
enable_pin: PB10
max_power: 1.0
shutdown_speed: 1.0 # Always keep the fan on at full power
does this make sense ?
Why are you doing this? Rat-OS already configures this for you by default
oh
which pin do i need t oput it in
controller fan >?
BTW, Controller fans will only come on when the a stepper driver is active
so i have to plug it in
the controller fan ?
I got it
nioce
thanks for all the help
ill put it in performance mode now
and i will test it out
OKe turning on performance mode gave me a otp warning
Over temp?
yeah
But I just want no layer shift i dont really care that much for performance mode
Just to go over all the things ive done. I greased my bearings v rails etc
I checked belt tension its normal not tight at all. Rather loose but also not too loose
Ive added an fan over the steppers
i have turned performance mode on but off again because of the warnings
im now going to check my z offset again and then print another longer print
see what is going to await me tomoorrow morning
but im expecting more wasted filament :*(
They go hand in hand. You can't do normal accelerations without performance mode. As I said "performance mode" really is the normal current level
Non-performance is training wheels. Really shouldn't be getting overheating if a fan is vaguely pointed at the drivers. Do you have the correct driver's selected?
I left it all at stock
i checked
and steppers all btt tmc 2209
@TheTik @blacksmithforlife so ive messed up I unplugged the stepper while the power was still on. Probably frying that plug so motor 0 and 1 do not work . What ive done to diagnose the motor is i plugged the stepper and motor from 0 to motor 3 and 1 to motor 4. ive changed the config . and that all works
the motors work now
but
when i move on the y both y and x move
if i move on the x
same
im confused as hell
The middle motor slots are tied together on the octopus I believe
only motor 2_1 and motor 2_2
I checked i only blew up motor 0 appearantly
motor 1 still works
the input
and motor 3 and 4 arent being used so i would like to use one of them for my left rear motor