DC slammed on Homing after Set Kinetic Centre

If you set kinetic center and then try to Home, the T0 will home fine however DC will get slammed at the end stop. The only way to avoid this is to restart firmware. VCore4 300mm nothing crazy in the config.
Solution:
that is what set kinematic center does. It says to the printer - ignore everything you are at 250,250,250 (assuming a 500mm printer). So then when you home, it tries to move 250mm in all directions as you told it to
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4 Replies
Solution
blacksmithforlife
that is what set kinematic center does. It says to the printer - ignore everything you are at 250,250,250 (assuming a 500mm printer). So then when you home, it tries to move 250mm in all directions as you told it to
letniq
letniqOP17h ago
I don't think this is correct. After I hit the home button. T0 is moved at the normal homing speed and it stops at the end stops. T1 is slammed at very high speed nothing to do with the normal homing speed. In case T1 is at the end stop when you hit home you can clearly hear the belt skipping.
blacksmithforlife
GitHub
RatOS-configuration/macros/util.cfg at v2.1.x · Rat-OS/RatOS-config...
The RatOS modular klipper configuration. Contribute to Rat-OS/RatOS-configuration development by creating an account on GitHub.
letniq
letniqOP17h ago
I understand what the macro does however I believe when I hit home button it should home both heads correctly. Even in the macro is written to do G28 after your done. However G28 (Homing) is not working correctly

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